Colleen Mondor Profile picture
May 9 15 tweets 5 min read
The NTSB has released the docket & factual report for the Nov 2019 plane crash in SD that killed 9 and injured 3. This is going to be mostly about the pilot's failure to fully deice the aircraft but I've got additional thoughts. 🧵 nytimes.com/2022/05/09/us/…
This was a corporate aircraft flying corporate officers & family who had been hunting at a lodge for several days. More on those folks & the company can found in this ID article. eastidahonews.com/2019/11/kyani-…
The pilot had 2300 hours. He was a multi-engine, IFR pilot flying a single-engine PC12 aircraft. According to docs with the investigation, he worked for the company. He & another pax flew in the night before the crash. They were out the next morning brushing off the plane.
Everything about this witness statement & the deicing is bad. They could not reach the tail.

I'll say it again - they could not deice the tail.
Several outlets are reporting the a/c was overweight. (The report says about 107 lbs over.) More importantly, it was loaded 3.99-5.49 inches aft CG. When you add that to ice on the tail you get a predictable nightmare scenario - a/c stall on takeoff, which is what happened.
We need to talk about pressure, however. This is a fairly low time corporate pilot. The CVR has some interesting interactions between the PIC and the airport manager who was plowing. He told the PIC not to go. (RDO1 = the pilot, APT = mgr)
More between the manager & PIC. (The PIC had obtained an IFR clearance via cell phone to depart - there is no tower at this airport.) Now we also have a passenger chiming in - HOT-1 is the PIC talking to everyone else.

The airport manager was so frustrated.
And then we've got this. They took off & realized right away they were in trouble. (HOT2 was the front seat passenger.)
He couldn't pull it out - no one could. Aft loaded, tail heavy from ice. He knew right away.
From a witness, on conditions at the airport.
From the factual report. This is just....
And here's the weather from the factual. A more detailed report is in the docket. But, you get the picture from this.
There are no interviews with a corporate flight dept in the docket. I have no idea if this pilot just answered directly to the passengers or anyone else. He told the lodge owner they had to go back that day. The report does not ask why he said that. This will be pilot error.
I don't understand why the pilot chose to takeoff in these conditions but I can't help but think it was not entirely his decision - or even partly his decision. Part 91 corporate flying often takes decision-making out of the cockpit. And there's nothing that will change that.
At the very least I wish the NTSB would question the corporate officers/mgmt & any existing flight dept to determine how the decision-making process occurs. They did not do that here (it appears) and that seems like a missed opportunity to shed some light on a big problem. /end

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Oct 30, 2020
An Alaska crash story #6
Ryan Air Service FAR Part 135 commuter/air taxi
Nov 23, 1987
18 fatalities, 3 serious injuries
PIC total time 7087 hrs; 5134 make/model

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Investigation closed. (NTSB pic) /1
The probable cause was determined to be due to the flight crew’s actions, both of whom died in the crash. There were multiple other factors involved in this accident however, involving both the company & the FAA. /2
At the time of the crash, Ryan Air was Alaska’s largest Part 135 operator. It flew 29 aircraft, employed 250 people and operated out of 8 bases to 85 different airports statewide. It’s history dated back to the 1950s. /3
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An index of my recurring tweet series on Alaskan Crash Stories. This will be updated with new entries as I continue to analyze commercial aviation accidents in the 49th state.
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An Alaska crash story #3
Hageland Aviation dba ERA Alaska FAR Part 135 commuter/air taxi
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adn.com/alaska-news/20…
You may know ERA Alaska (& specifically Hageland Aviation) from the “reality” tv show, “Flying Alaska Wild”. FYI: A lot of this show was not true. (Starting with the fact that Jim Tweto was the company’s minority owner.)



Now, back to the crash. /3

go.discovery.com/tv-shows/flyin…
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